Author Topic: Feedback current transformer doesn't work  (Read 17034 times)

Offline nick

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Feedback current transformer doesn't work
« on: November 21, 2019, 01:38:13 PM »
Hi,

I've built a coil using Loneoceans' SSTC 2 https://www.loneoceans.com/labs/sstc2/sstc2schematicv10.jpg. My circuit is the same for all intents and purposes. The only difference - and source of my problem - is the feedback current transformer. In short, nothing works when using ~50 turns around a core through which the bottom of the secondary passes (as described in the linked schematic). What's interesting is that when I use an antenna instead (which works GREAT) and scope the output of the CT, I see exactly what I expect: the coil's resonant frequency at more than sufficient voltage. Any ideas what the problem could be?


To hijack my own post, I had another question - where can one find a nice toroidal top-load? I'm currently using 2 smooth salad bowls glued together (lol) - which works OK - but would love to have something nice like in Loneoceans' coil: https://www.loneoceans.com/labs/sstc2/toroid.jpg

Thanks!

Offline Weston

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Re: Feedback current transformer doesn't work
« Reply #1 on: November 22, 2019, 02:43:03 AM »
Have you tried reversing the phasing of the current transformer? That would be my first guess.

The three places I know where you can get toploads from are ebay, information unlimited (amazing1), and eastern voltage research. They are somewhat pricey, after years of making tesla coils I recently bought my first real spun aluminium topload.

Offline nick

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Re: Feedback current transformer doesn't work
« Reply #2 on: November 22, 2019, 11:58:46 AM »
Thanks for the reply! I'm sure I've tried reversing the polarity but will do so again tonight. Unfortunately I'm pretty sure I've already done this and it didn't work :(

I'm kind of getting tired/bored of my current build (it always feels like the journey is so much more fun than the destination...) so I think this weekend I will upgrade to a full H bridge. I now have 9 or 10 60n60 IGBTs - I might as well put them to work!

Shame about the (lack of) availability of nice toroids... My next step might be to try aluminium ducting that I see others use but I'm surprised that the relatively rough surface works well.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #3 on: November 24, 2019, 02:58:48 AM »
I was just looking at that SSTC schematic with current feedback to answer another post.  It appears to me to have an error.  The two 1N4148 clamp diodes on the current transformer secondary should be on the HC74 input (pin 1) rather than directly on the transformer secondary.  Even better would be to add a second 1k resistor in series with the HC74 input, then place the clamp diodes between the two resistors:
 [ Invalid Attachment ]

Does anyone else have experience with the "http://www.loneoceans.com/labs/sstc2/sstc2schematicv10.jpg" circuit with CT feedback?  Anyone have a reason that it makes sense to have a diode directly across the CT, making it carry a net DC current?
David Knierim

Offline Mads Barnkob

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Re: Feedback current transformer doesn't work
« Reply #4 on: November 25, 2019, 09:11:13 AM »
It could just be a copy/paste error from the Steve Ward SSTC5 / mini SSTC that he used as inspiration. The antenna single-wire feedback was suddenly replaced by a two-wire CT and it just got referenced to ground.



The diodes are there for clamping the induced high voltages on the antenna, since corona on the antenna is pretty normal, maybe he is just missing a DC blocking capacitor like Steve Ward uses with the CT feedback here:

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Offline nick

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Re: Feedback current transformer doesn't work
« Reply #5 on: November 25, 2019, 10:23:17 AM »
Thanks both! Will try this tonight.

Offline nick

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Re: Feedback current transformer doesn't work
« Reply #6 on: November 25, 2019, 05:55:49 PM »
Hello again, apologies for another reply. And also apologies for the noobish question but could you perhaps explain why it would make a difference whether you put the DC blocking cap before or after the diode clamp? Wouldn't it be OK that the cap removed the DC bias regardless, as long as it's in front of the 74HC? What am I missing?

Also @davekni - it would be much appreciated if I could get your feedback as to why adding another 1k resistor will help? I am even wondering why a resistor is needed at all give the CT feedback should produce a low current (albeit at high voltage, but that's what the clamp is for)? Further, why is it beneficial to have another 1k resistor in series - what should this accomplish?

Thank you!

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #7 on: November 26, 2019, 04:30:23 AM »
That's a good question.  Transformer windings (and inductors in general) have zero DC voltage across them (ideally - ignoring wire resistance).  In other words, the average voltage is zero.  That's because the current through an inductor is the integral of the voltage across it (scaled by 1/inductance).  If the average voltage is positive, current will ramp up until it pulls the average back to zero.

With the diodes clamping the CT output directly, the negative voltage is clamped to ~-0.7V (one diode forward drop).  The positive voltage is clamped to +5.7V.  This ramps CT current up until the duty cycle is lopsided enough to make the negative clamp time ~8 times as long as the positive part to get zero average.

BTW, here's the attachment that failed previously, basically the same as what Mads posted, except the cap and resistor are reversed, which makes no difference.  Hopefully it shows up this time.


Note R2 in the second schematic Mads posted.  That helps kick-start oscillation.  Putting the resistor (R2) between pins 1 and 2 of the HC14 should work instead.  That has the advantage of repeated kick-starting if the first one fails.

I'd also suggest an additional resistor between HC14 pin 1 and the clamp diodes D1/D2, ~1k ohms.  That further reduces current to the HC14 input, forcing the clamp diodes to handle most of the current when voltage exceeds 0-5V.
David Knierim

Offline nick

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Re: Feedback current transformer doesn't work
« Reply #8 on: November 26, 2019, 12:48:05 PM »
It works! Thanks guys! I ended up with one end of the CT in series with a 100n cap which is followed (in series) by a 1k resistor, before hitting the diode clamp. The other end of the CT is obviously grounded. I did all this before seeing your latest reply Dave, so will try the additional R tonight.

By the way, I still have another 100n DC blocking cap AFTER the clamp - any point keeping it there?

To be entirely honest, I'm struggling to understand all the theory in your post Dave from a first read, but that makes me happy since I can research myself / do simulations, and hopefully learn something new :)

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #9 on: November 27, 2019, 06:16:11 AM »
I'd suggest removing the second blocking cap - it's the perfect place for a second 1k resistor.  BTW, the second resistor should not affect performance, just reduce HC14 input current in high-power situations, improving reliability.  (As it stands, the HC14 pin 1 is not at a defined DC level because of the second cap.  The HC14's internal input clamp diodes conduct once oscillation starts, making that second coupling cap voltage go to roughly zero.)

The startup issue is this:  When the enable pulse comes, the gate drive transformer is driven to one state or the other (one pair of H-Bridge FETs turned on).  Depending on what charge is left on the H-Bridge output DC blocking capacitor, that initial state may or may not generate much current (or voltage, so this applies to antenna feedback too).  Mads suggests adding a ~5-10k power resistor across the H-Bridge output, at least for DRSSTCs.  (For SSTCs, across the DC blocking capacitor works too.)  This makes the initial H-Bridge output state centered, so the initial enable edge generates a half-voltage edge.  That single half-voltage edge must generate enough current signal to change the HC14 state, which then makes another H-Bridge output transition, making another current half-cycle, etc.  (Oscillation starts.)

R2 in the second circuit Mads shared does two things.  It defines the DC level of the HC14 input between enable pulses.  It then changes the level on the HC14 input after the enable edge.  That makes a full-voltage H-Bridge output transition to initiate oscillation.  If R2 were placed across the HC14 (pins 1 to 2), then the HC14 will oscillate even without enable, so will create H-Bridge edges after enable goes true, until oscillation takes over.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #10 on: May 22, 2023, 09:18:05 PM »
Hey guys, how are you doing?
I'm having the same problem on my RSSTC. Once again I'm following one of Zach's from Labcoatz tutorials.
Link: https://www.instructables.com/Building-the-Worlds-Easiest-QCW-Tesla-Coil-Staccat/

My circuit is working and I already got good results using the antenna, however I am having “bad” output with unstable BPS and pulse width.
-



Because of this I would like to try using a feedback transformer.
On the PCB designed by him there is already a connection for the antenna and for the CT. The scheme is as follows:
-


I tried using two different CTs (Also reversing the polarity). One of them I took from another SSTC (About 25 turns). The other one I wound around a ferrite core I took from an old computer power supply (about 55 turns).
-


My coil is currently in this setting
-

-

-
I'm using the CT at about that position.
-


When I'm using just the antenna I can hear the ucc clicking at the frequency of the 555 interrupter, when using the CT I can't hear anything.
I found this topic and decided to ask here because it is something related. I don't have much experience so I might be missing something very obvious.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #11 on: May 23, 2023, 04:16:15 AM »
Have you tried adding the 10k startup resistor from Steve's DRSSTC-.5 schematic Mads posted above?  Also helps to have bleed resistor(s) across primary coupling cap(s) to make sure half-bridge output is at center supply (both FETs have equal Vds before burst starts).

Quote
The other one I wound around a ferrite core I took from an old computer power supply (about 55 turns).
How do you know this core is ferrite?  Most supply toroid cores are powdered iron (or iron alloy).  The input line common-mode choke core will be ferrite, if that is what you pulled from supply.  Other cores are likely not ferrite and not suitable for CTs.

Any picture with CT actually connected?
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #12 on: June 19, 2023, 03:36:20 PM »
I made some tests and changes.

Quote
The other one I wound around a ferrite core I took from an old computer power supply (about 55 turns).
How do you know this core is ferrite?  Most supply toroid cores are powdered iron (or iron alloy).  The input line common-mode choke core will be ferrite, if that is what you pulled from supply.  Other cores are likely not ferrite and not suitable for CTs.
Any picture with CT actually connected?
Really I wasn't sure if this core was ferrite, so I used the core that came on a Chinese SSTC board. Originally this CT had 25 turns, but I redid it and now it has over 50.

With the 10k resistor between 74HC14 pin 13 and before the clamp diodes coil works as if it were in CW mode (using the new CT).

In other tests I kept the resistor but used the antenna instead of the CT. With this configuration the coil worked, but with a very weak output.


Without the resistor and with the new CT the coil didn't work, but I noticed that when turning on the main voltage sometimes I got a small discharge on the output, but the coil didn't keep the oscillations.



-

And here it works with just the antenna.


Any other ideas of what could be causing these issues?

Offline NyaaX_X

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Re: Feedback current transformer doesn't work
« Reply #13 on: June 19, 2023, 04:19:21 PM »
I guess.. I don't know if this will work.

Make a Faraday cage to cover the driver. And connect the cage to Ground.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #14 on: June 19, 2023, 07:38:57 PM »
Quote
Make a Faraday cage to cover the driver. And connect the cage to Ground.
I'd suggest the same.  For testing, a cardboard box covered in aluminum foil works well.  I'm not thinking of any other possible causes for your symptoms than electrical interference from coil to driver board, so grounded shielding should help.  If problems persist, at least the shielding will also make future scope captures cleaner.

The suggestion Zak posts below is great for startup issues, especially for coils like this starting when line voltage is low.

Quote
coil works as if it were in CW mode
This is the issue that seems likely to be caused by interference from secondary voltage.  Almost any grounded shielding around driver board helps.  I use a 5-sided box (no top cover) with driver ~6cm below top.  Allows scope probing from top and provides sufficient shielding.
Other less-likely possibility that comes to mind is some bad connection within driver/interrupter circuitry, bad solder joint or poor socket connection if you use any sockets.
« Last Edit: June 19, 2023, 10:14:54 PM by davekni »
David Knierim

Offline ZakW

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Re: Feedback current transformer doesn't work
« Reply #15 on: June 19, 2023, 08:51:19 PM »
Hello TiagoBS,

Sorry to hear you are experiencing this problem, you are not alone though! I had this exact same issue recently (several times throughout different version too).

For me the problem with the output and feedback happened after I killed the IGBTs after that I could not get the coil to output consistently and it would have the light snapping arc sound. Bringing my hand near the CT would cause the coil to run sometimes. Disconnecting it completely would result in some output too. I replaced EVERYTHING on my board to no avail. What fixed it for me was adding a few components to the 74HC14 feedback section. This allowed the 74HC to self oscillate and trigger the coil to turn on. Here is the example from my thread:


I ended up making C3 220pf and R13 11kohm to output around 400kHz. If you want to try this you can set C3 to a low value like 220pf (depending on target frequency) and then use a potentiometer for R13. Check what the oscillation frequency is and adjust the pot so it is slightly below what your coil runs at. Don't forget R10 as well, the additional burden resistor really helped to improve the signal from the CT.

Here is a link to the post showing some scope captures of the coil failing to oscillate https://highvoltageforum.net/index.php?topic=2338.msg17153#msg17153. If you go to the third page you can see after I added the self oscillation the coil runs great now.

Good luck, the issue is really frustrating. I hope this helps.

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #16 on: September 21, 2023, 10:44:08 PM »
Hey guys, thanks for the help!

I added the self oscillation circuit and was able to measure and vary this frequency (320khz). I added the other components as suggested too.
I also made a Faraday cage.

C3 = 200pf
R13 = 22K - (Potentiometer)


-



I measure the frequency via pin 4 of the 74HC14, but in my last tests I was unable to read the signal (Likewise, I can't measure the signal from the interrupter), in addition to being very noisy signal.
-


Measuring GS of the two IGBTs with just the logic part powered, these were the readings:
I don't understand why they are so different.
-

-



When connecting the coil in this configuration it works as in CW. With only the logic part turned on I can hear the UCC clicking on the interrupter frequency. By changing the value on the frequency potentiometer I can notice the increase or decrease in the clicking sound.

If I disconnect the self oscillation circuit the coil doesn't work and I can't hear the UCC clicking. However, when I put my finger on R1 it works (like in CW). With just the logic part connected, by touching R13 I can hear the UCC clicking very quickly, like at 60Hz.
« Last Edit: September 21, 2023, 10:47:43 PM by TiagoBS »

Offline ZakW

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Re: Feedback current transformer doesn't work
« Reply #17 on: September 21, 2023, 11:56:16 PM »
Sounds like you are making progress! I have complied A TON of notes on all the things I have learned and issues I have overcome with this type of coil. I plan on sharing all of it once I finish boxing my up my latest RSSTC coil. Mine is only a SSTC not dual resonant. Still though, the issues you described below are something I had as well. I will have to check my notes when I am home later.

Quote
I measure the frequency via pin 4 of the 74HC14, but in my last tests I was unable to read the signal (Likewise, I can't measure the signal from the interrupter), in addition to being very noisy signal.

Why were you not able to measure the interrupter output?

Quote
When connecting the coil in this configuration it works as in CW. With only the logic part turned on I can hear the UCC clicking on the interrupter frequency. By changing the value on the frequency potentiometer I can notice the increase or decrease in the clicking sound.

If I disconnect the self oscillation circuit the coil doesn't work and I can't hear the UCC clicking. However, when I put my finger on R1 it works (like in CW). With just the logic part connected, by touching R13 I can hear the UCC clicking very quickly, like at 60Hz.

Is the feedback signal overpowering the interrupter signal? I am not really sure how this could happen if the UCC is also connected to the interrupter. It would be helpful to see what the output of the interrupter looks like when it is exhibiting this behavior.

The only other thing I can think of at the moment is related to the ZCD. On several versions of my PCBs, my coils would start out working fine then I would have a failure and it would start exhibiting strange BPS/feedback issues similar to what is happening to you. In my builds I have used several different methods for detecting zero crossing. If the ZCD is not working or triggering properly the interrupter will not output and the coil shouldn't run. It may be that you have a second issue related to the ZCD/555 timers.


Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #18 on: September 22, 2023, 06:05:35 AM »
If I'm understanding your pictures correctly, one issue shows up there:  Shield for driver should be connected to ground including driver ECB ground.  Bottom of secondary should not connect to shield, not until after passing through CT.

Quote
I measure the frequency via pin 4 of the 74HC14, but in my last tests I was unable to read the signal (Likewise, I can't measure the signal from the interrupter), in addition to being very noisy signal.
Not sure what you mean by "unable to read the signal".
Noise is unexpected.  Is the H-bridge powered for this measurement of 74HC14-4?  Or is this with only logic powered?

Quote
Measuring GS of the two IGBTs with just the logic part powered, these were the readings:
I don't understand why they are so different.
That is more different than I'd expect, but perhaps reasonable.  74HC14 input threshold voltage is usually a bit below 2.5V (below half of supply voltage).  Your chips must be quite a bit below 2.5V.  Are you certain your chip isn't 74HCT14?
This duty cycle error (not 50%) can be fixed by adding another resistor, either across D2 or from 74HC14-1 to ground.  That lowers the input signal level to be centered around 74HC14 input logic threshold.  Resistor value needs to be adjusted to get 50% duty cycle.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #19 on: September 22, 2023, 07:53:07 PM »
I did some more tests.

Why were you not able to measure the interrupter output?

Well, it looks like there's a problem with both 555s (It's not the first time this has happened). I swapped the two and was able to read these waves:
On one of the pins of the 100k potentiometer (interrupter frequency).
-


These here are from the interrupter output:
-

-

-


Low voltage transformer (Disconnected from PCB)
-


Connected to PCB:
-


I believe I need to resolve this noise issue before proceeding. It's disturbing all my readings.


The only other thing I can think of at the moment is related to the ZCD
Maybe I need to change some components on the board, maybe the 2N2222?

If I'm understanding your pictures correctly, one issue shows up there:  Shield for driver should be connected to ground including driver ECB ground.  Bottom of secondary should not connect to shield, not until after passing through CT.
I will make this change.


Noise is unexpected.  Is the H-bridge powered for this measurement of 74HC14-4?  Or is this with only logic powered?
Only logic powered.

That is more different than I'd expect, but perhaps reasonable.  74HC14 input threshold voltage is usually a bit below 2.5V (below half of supply voltage).  Your chips must be quite a bit below 2.5V.  Are you certain your chip isn't 74HCT14?
Wow, once again you got it right!
My chip is actually the HCT14. But I have some HC14 too. I'll make the change and test the result.

About the difference between the two, I found it briefly in a search that:
The basic difference is that HCT14 are designed to work at lower inputs (5v) and HC are rated for higher inputs (15v).

How does this affect the feedback operation?

This duty cycle error (not 50%) can be fixed by adding another resistor, either across D2 or from 74HC14-1 to ground.  That lowers the input signal level to be centered around 74HC14 input logic threshold.  Resistor value needs to be adjusted to get 50% duty cycle.
Did you identify this from the image with the blue wave?



Offline Egg

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Re: Feedback current transformer doesn't work
« Reply #20 on: September 22, 2023, 09:20:18 PM »

How does this affect the feedback operation?


Did you identify this from the image with the blue wave?


Like david said it causes the duty cycle to go higher than 50%. You can see this both on the blue and yellow reading that the duty cycle is like %70/%30 percent. It seems easier to me to just get the right ic instead trying the resistor opiton. Can you scope the voltage on the 12v and 5v rails? See if there is any noise?
« Last Edit: September 22, 2023, 09:42:59 PM by Egg »

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #21 on: September 22, 2023, 09:51:07 PM »
Quote
I believe I need to resolve this noise issue before proceeding. It's disturbing all my readings.
Yes, I'd agree.  Most of the scope traces can be interpreted even with noise present.  However, whatever is causing noise may be interfering with circuit operation at times.
Noise may be high frequency oscillation of some part of your circuit, which is aliasing with scope sample frequency.  Would be good to expand horizontal way out (low time/div) when looking at noise.
Try scoping ground on your board.  Both probe ground clip and probe tip connected to ground.  You may pick up enough of the noise that way.  Presuming so, noise is much easier to see when by itself and not on top of some other signal.

Quote
Wow, once again you got it right!
My chip is actually the HCT14. But I have some HC14 too. I'll make the change and test the result.

About the difference between the two, I found it briefly in a search that:
The basic difference is that HCT14 are designed to work at lower inputs (5v) and HC are rated for higher inputs (15v).
Neither can handle 15V.  Only the original 74C14, not HC nor HCT.  Both HC and HCT work well at 5V.  The difference is that HCT is designed for logic inputs coming from conventional TTL with input thresholds specified as being between 0.8V and 2.0V.  HC is expecting to be driven by other CMOS logic at the same 5V supply.

Quote
How does this affect the feedback operation?
Because HCT input thresholds are low, it takes a short time for the input capacitor to charge up the rising threshold, but a long time for it to discharge back below the falling threshold.

Quote
It seems easier to me to just get the right ic instead trying the resistor opiton.
Agree.  Even 74HC14 threshold voltages are typically somewhat lower than centered around 2.5V, though not nearly as low as 74HCT14 thresholds.  If you want to be perfectionist, a resistor still helps.  A higher value will work with the correct 74HC14 chip.
David Knierim

Offline ZakW

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Re: Feedback current transformer doesn't work
« Reply #22 on: September 22, 2023, 10:22:28 PM »
Quote
Maybe I need to change some components on the board, maybe the 2N2222?

Before you change more parts can you scope the low voltage AC transformer output and the output of your interrupter? By scoping an AC signal you can compare it against the output of the interrupter. That helps confirm if the ZCD is triggering at or around zero crossing as well as making sure the interrupter is outputting a corresponding signal. From your included scope capture it looks like it is outputting a signal its just hard to tell if it is sync with the mains.

To reiterate, I was not able to get the coil to run consistently or at all without the self oscillation mod to the 74HC feedback section. If you're able to confirm that the above is working correctly, your issue may be more related to the 74HC chip as others have mentioned.

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #23 on: September 26, 2023, 01:45:51 AM »
Well, today I did some more tests.

Starting with the full bridge.

This first image is the reading of the rectifier output (using the 12v transformer).
-



Here after I put my finger between the bridge output. (It seems more correct).
-


The following two images are readings of the negative output of the rectifier bridge and the two phases of the 12v transformer.
-

-



I wanted to confirm whether this behavior is expected because when I carried out the same measurements in mains voltage (without the finger part) with the same bridge I got the expected result, but using the 12v transformer it did not.

After confirming this I will continue testing the other components to identify the source of the noise.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #24 on: September 26, 2023, 05:05:33 AM »
Quote
This first image is the reading of the rectifier output (using the 12v transformer).
To get a meaningful signal from the rectifier output, you need some load current, such as a resistor of 1k or lower.  Otherwise slight leakage current or capacitance of rectifier diodes overcomes tiny current of 10M scope input.

I can't quite read the low-res schematic image from LabCoatz.  The resistor on AC input after 1N4148 diode looks like perhaps 100k.  That may be too high if diode bridge has much leakage current.  I'd replace with 1k or lower and then scope again.  Diode leakage current and minimal load may be causing your line timing issues.
David Knierim

Offline ZakW

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Re: Feedback current transformer doesn't work
« Reply #25 on: September 26, 2023, 06:38:13 AM »
TiagoBS,

Here are a couple old scope captures of the interrupter running relative to a 12v transformer. Ignore the blue trace. I would check this to verify if my interrupter was outputting the correct signal relative to the ac half cycle. Can you verify this as well? Were you able to implement the components that I shared in my previous post? I added an updated screenshot as well. I ended up using a 220pf cap and a 11k resistor to get the correct oscillation frequency. 1nf should work it is just a matter of choosing the corresponding resistor value to achieve the desired freq.

Yellow = Interrupter output
Purple = reference AC signal


Purple = Interrupter output
Yellow = reference AC signal


« Last Edit: September 26, 2023, 06:21:17 PM by ZakW »

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #26 on: September 28, 2023, 09:40:55 PM »
Well, I redid the entire board just in case.
It's still working like it does on CW.

During the process I checked the noise as I added the components.
The measurements were made only with the two 555 and the UCC37322 (as I only got this chip in SMD and had to solder it permanently)
When all components are connected, all the measurements are very noisy (all tests were only with the logic part connected)


I took some readings from the oscilloscope.

One phase of the mains voltage and pin 3 of the 555.
-

-

Pin 4 of the 555 at the highest and lowest duty cycle respectively.
-

-


Pin 6 of the 555 (here with little noise)
-

-


This reading here was done on the ground wire (disconnected from de board). Only with the positive test tip.
-


My apartment is very close to one of the energy distribution stations in my city. Many high voltage cables pass through my street, both on lampposts and underground. I'm using a large metal fence as the ground. Maybe this is picking up some interference.
When I took measurements using the connected ground the noise seemed to get much worse.

TiagoBS,
Were you able to implement the components that I shared in my previous post? I added an updated screenshot as well. I ended up using a 220pf cap and a 11k resistor to get the correct oscillation frequency. 1nf should work it is just a matter of choosing the corresponding resistor value to achieve the desired freq.
Yes, I added the components and switched from the 74HCT14 to the 74HC14. I left a 100k potentiometer to change the frequency.
In this capture the card was showing a little more noise.
-

-



At times the noise seems much more intense, changing the waveform. Here I took a measurement with the test tip loose with just the ground connected to the negative on the board.
-

-


I can't quite read the low-res schematic image from LabCoatz.  The resistor on AC input after 1N4148 diode looks like perhaps 100k.  That may be too high if diode bridge has much leakage current.  I'd replace with 1k or lower and then scope again.  Diode leakage current and minimal load may be causing your line timing issues.
Here is a link with better resolution:
https://content.instructables.com/ORIG/FFF/UMFD/L1AQ3MJU/FFFUMFDL1AQ3MJU.png
-


Is this resistor marked in yellow?

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #27 on: September 28, 2023, 11:01:20 PM »
Quote
One phase of the mains voltage and pin 3 of the 555.
There are two 555 chips in the schematic.  Don't now how to interpret scope plots without knowing which 555 chip is being probed.  Perhaps call them "left" and "right" 555 chips per their position in schematic.  (Unfortunate that this schematic does not include reference designators, such as R1 or U1.)

Quote
Is this resistor marked in yellow?
Yes.  I recommend a lower value such as 1k instead of 100k.  As low as you have around without exceeding power dissipation limit of resistor.  That will reduce sensitivity to both diode bridge leakage current or noise.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #28 on: September 29, 2023, 12:30:30 AM »
Quote
One phase of the mains voltage and pin 3 of the 555.
There are two 555 chips in the schematic.  Don't now how to interpret scope plots without knowing which 555 chip is being probed.  Perhaps call them "left" and "right" 555 chips per their position in schematic.  (Unfortunate that this schematic does not include reference designators, such as R1 or U1.)
I'm sorry about that. The measurements were taken at left 555.
Only the ramp waves were capture at 555 on the right.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #29 on: September 29, 2023, 07:15:19 PM »
Quote
This reading here was done on the ground wire (disconnected from de board). Only with the positive test tip.
If you have no other connection between your board and line ground, then that 60Hz line frequency signal is expected and would show up anywhere.  Capacitance through 12V transformer or other power supply to line is enough to make that +-5V line frequency signal.  The noise in many of your other scope traces is much higher frequency, above your ~350kHz SSTC operating frequency.  Measuring with scope probe ground clip disconnected will not be useful in finding that high frequency noise source.  Measuring with both scope ground clip and probe tip connected to ECB "ground" may be useful.

Quote
Pin 4 of the 555 at the highest and lowest duty cycle respectively.
Looks like duty cycle adjustment has no effect.  Perhaps 100k POT to the right of right 555 is the wrong value or shorted.
Also, did you change which side of 12V transformer is being scoped for line voltage reference?  Does not match previous plot of pin 3.

Quote
Yes, I added the components and switched from the 74HCT14 to the 74HC14. I left a 100k potentiometer to change the frequency.  In this capture the card was showing a little more noise.
Looks good, other than noise.  What does this look like with horizontal expanded as much as possible, say 10ns/div or how ever fast your scope can go?  The noise is likely so high frequency that it is aliasing with scope sample frequency.  I'd guess either you are near some RF communication equipment or a part on your board is oscillating at high frequency (driver chips would be most likely for that).

Quote
At times the noise seems much more intense, changing the waveform. Here I took a measurement with the test tip loose with just the ground connected to the negative on the board.
Again, line frequency noise is normal if either probe tip or ground are not connected.

Quote
Here is a link with better resolution:
Thank you for the better link.  Makes analysis and discussion easier.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #30 on: September 29, 2023, 09:00:54 PM »
Well, I did more tests this morning. I can't find what I changed, but the coil is now working with the CT!


Looks like duty cycle adjustment has no effect.  Perhaps 100k POT to the right of right 555 is the wrong value or shorted.
Also, did you change which side of 12V transformer is being scoped for line voltage reference?  Does not match previous plot of pin 3.

Here are some captures of the duty cycle changing and also the noise in the signal.
I changed the pin that was measured from 3 to 4. I believe this caused the difference in readings.
-

-

-


Looks good, other than noise.  What does this look like with horizontal expanded as much as possible, say 10ns/div or how ever fast your scope can go?  The noise is likely so high frequency that it is aliasing with scope sample frequency.  I'd guess either you are near some RF communication equipment or a part on your board is oscillating at high frequency (driver chips would be most likely for that).

Here is a capture at 10ns/div
-


In this video the 74HC14 is self oscillating at 100khz. I read this in ZakW's thread:
Quote
Ideally self-oscillation frequency will be close to operating frequency, about 3x higher than now.  330pF would be roughly there.  However, better to go down to 220pF and increase R13 value to get back down to 450kHz.  Better to have some margin away from self-oscillation dropping out.  (Likely going to very high frequency rather than dropping out, too high to get through driver chip.  Could cause problems, so better to stay away from failure threshold.)
Since the coil oscillation takes over the self-oscillation of CH14, what is the difference between leaving it oscillating at 100 kHz and increasing it to close to the coil's operating frequency?

I also read the ramp on pin 6 of the 555 on the right
-
 [ You are not allowed to view attachments ]

And here is the reading of the mains phase that is going to the interrupter and the Gate of one of the transistors.
-
 [ You are not allowed to view attachments ]

Quote
Yes.  I recommend a lower value such as 1k instead of 100k.  As low as you have around without exceeding power dissipation limit of resistor.  That will reduce sensitivity to both diode bridge leakage current or noise.
I haven't changed the resistor yet. But I will exchange it and measure the difference
« Last Edit: September 29, 2023, 09:13:11 PM by TiagoBS »

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #31 on: September 30, 2023, 01:43:06 AM »
Quote
Here are some captures of the duty cycle changing and also the noise in the signal.
OK, I now see that you were changing duty cycle by changing on time, not by changing off time.  Previous scope captures of left 555 pin 4 would be affected only by off time adjustment (100k POT to right of schematic).  Thus I'd presumed you were adjusting that POT.  Makes sense now, as left 555 pin 4 is not expected to change with left 20k POT.

Quote
I changed the pin that was measured from 3 to 4. I believe this caused the difference in readings.
I saw that.  However, still doesn't fit.  Pin 4 is a low-true reset to 555 chip.  When pin 4 is low, pin 3 is also low.  However, pin 3 goes high during low line half-cycles.  Pin 4 is high only during high line half-cycles.  So something else changed between those two captures.

Quote
Here is a capture at 10ns/div
That looks like ring more than noise.  Perhaps a capture at 100ns/div would be better for showing noise.

Quote
Since the coil oscillation takes over the self-oscillation of CH14, what is the difference between leaving it oscillating at 100 kHz and increasing it to close to the coil's operating frequency?
As long as a single edge is sufficient to start oscillation, 100kHz is likely fine, or even 0Hz (no self-oscillation mod).  Two advantages of self-oscillation closer to operating frequency.  First, in case feedback signal is weak, allows feedback to grow for a cycle or two until it is strong enough.  Second, higher frequency minimizes voltage across 1uF GDT coupling capacitor and minimizes chance of GDT core saturating during the initial half-cycle before oscillation starts.

Quote
I also read the ramp on pin 6 of the 555 on the right
Noise looks worse during time when coil is running (driver chips switching state).  Suggests at least some of the noise is coming from driver chips.  Does your ECB have a ground plane?

Quote
And here is the reading of the mains phase that is going to the interrupter and the Gate of one of the transistors.
Looks appropriate for a long (half cycle) on-time.  BTW, extending past 1/4 cycle usually does not add to arc length, but can make arc thicker by keeping it energized longer.

Might be a good idea to increase right 100k POT setting to reduce repetition rate.  Would allow playing with on-time while still keeping duty cycle low, so minimize stress on IGBTs and gate drivers in case of issues.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #32 on: October 04, 2023, 07:00:42 PM »
Quote
Yes.  I recommend a lower value such as 1k instead of 100k.  As low as you have around without exceeding power dissipation limit of resistor.  That will reduce sensitivity to both diode bridge leakage current or noise.

I replaced the 100k resistor with a 680ohm one and took this reading with the oscilloscope after the change. I don't know if this change affected it, but now the reading is much less noisy.

That looks like ring more than noise.  Perhaps a capture at 100ns/div would be better for showing noise.
-

-



Quote
Noise looks worse during time when coil is running (driver chips switching state).  Suggests at least some of the noise is coming from driver chips.  Does your ECB have a ground plane?
It does not have.

Looks appropriate for a long (half cycle) on-time.  BTW, extending past 1/4 cycle usually does not add to arc length, but can make arc thicker by keeping it energized longer.
Might be a good idea to increase right 100k POT setting to reduce repetition rate.  Would allow playing with on-time while still keeping duty cycle low, so minimize stress on IGBTs and gate drivers in case of issues.
Do you mean changing the 100k potentiometer that controls the frequency for example with a 500k one?
And how would this affect the duty cycle and allow playing with on-time?

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #33 on: October 05, 2023, 05:58:19 AM »
Quote
I replaced the 100k resistor with a 680ohm one and took this reading with the oscilloscope after the change. I don't know if this change affected it, but now the reading is much less noisy.
Nice that the noise amplitude dropped a bit.  These two scope captures at 500ns/div and 2us/div are perfect for seeing the noise detail.  There are two frequencies present, one at ~6.5MHz and another around 600kHz.  The lower frequency ~600kHz component may be ringing from your coil upper pole or primary wiring or etc.  Upper frequency is more concerning.  Most likely some component on your board is oscillating at 6.5MHz.  (Unless you live near a radio transmitter or some other equipment generating 6.5MHz.)  You can use your scope probe as a magnetic pickup probe by connecting ground clip to probe tip and moving that loop around your circuit in search of 6.5MHz noise.  Or, for better location precision, wind a few small turns of wire between scope tip and ground clip.

Quote
Quote

    Noise looks worse during time when coil is running (driver chips switching state).  Suggests at least some of the noise is coming from driver chips.  Does your ECB have a ground plane?

It does not have.

Quote from: davekni on Se
That may be root of noise issues.  High current chips such as gate drivers pull large current spikes from power pins and large current spikes charging output load capacitance.  Good short routing to bypass caps helps.  Some boards without ground planes (and even breadboard hand wiring) end up working.  Ground planes aren't an absolute necessity.  However, much more chance of problems without one.

Quote
Do you mean changing the 100k potentiometer that controls the frequency for example with a 500k one?
And how would this affect the duty cycle and allow playing with on-time?
No.  I mean adjusting the existing 100k potentiometer to a higher value.  As is you are getting one half cycle every two line cycles.  Setting 100k potentiometer to a higher value will increase that time.  Max 100k value should give you between one and two half-cycles per second.
David Knierim

Offline yourboi

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Re: Feedback current transformer doesn't work
« Reply #34 on: October 06, 2023, 02:05:03 AM »
I have been troubleshooting my zach armstrong MJOLNIR coil and I have developed the same issue. the feedback somehow ends up in the interrupter and exactly as you said it was working fine for a whole year of daily use.

Quote
Is the feedback signal overpowering the interrupter signal? I am not really sure how this could happen if the UCC is also connected to the interrupter. It would be helpful to see what the output of the interrupter looks like when it is exhibiting this behavior.

Quote
The only other thing I can think of at the moment is related to the ZCD. On several versions of my PCBs, my coils would start out working fine then I would have a failure and it would start exhibiting strange BPS/feedback issues similar to what is happening to you.

I don't have the time to read this thread too thoroughly right now. as I was troubleshooting my Mjolnir coil the past few weeks I have been debating posting here. I am pretty new to this all things considered. I've had this problem twice believe it or not on two separate boards. the antenna is finnicky to the touch placing my finger near the feedback antenna causes the interrupter to go super fast and ignore the enable pin. the interrupter seems to function fine with a perfect square wave. the Schmitt trigger looks good with its input being square. brand new ic and decoupling caps. sadly any readings I took show this on the output (Note: the noise goes away when I keep my hand away from the antenna, there is also a function generator connected to the antenna): https://imgur.com/a/XOgdTFT I've pretty much considered the coil as good as dead and am moving on to a new one because its taken abuse from troubleshooting and desoldering components. the problem started after pushing 2.2KVA through the thing and overheating and blowing the bridge up because the heatsinks I was using were even smaller then the typical ones. I went to rebuild and here we are.

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #35 on: November 16, 2023, 07:45:19 PM »
Well, I was already moving towards finishing this project. But once again there was a problem.
The coil was already working well, the self-oscillatory circuit working as expected.
However, when I assembled the coil in its final configuration I had problems with secondary interference. So I made a grounded shield out of cardboard and aluminum foil to separate the secondary from the PCB. This solved the interference problem. To give a better finish, I designed and 3D printed a new shield. When I went to test this new shield, I removed the resonant capacitors, the coil remained working. So I added the capacitors again and when I connected the coil it blew both transistors and the fuse.

They were my last two 60N65SMD.
Now I'm doing tests with IRFP460.

I placed the new mosfets and removed the resonant capacitors and I also had to change the ucc37321. But this time the output was very weak, with a neon indicator I can see the coil oscillating according to the interrupter, but with no visible output, even at the highest duty cycle it is possible to see just a small spark. I tried adding the resonant capacitors but with them the coil simply doesn't work, when removing the capacitors it starts working again with a weak output.

By turning on just the low voltage circuit it is possible to hear the ucc clicking according to the interrupter, but the click seems weaker and less audible than before.

Does anyone have any idea what could be happening?

Some photos of how the coil looked:


-

-

-

-

-

-

-

-
 [ Invalid Attachment ]

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #36 on: November 16, 2023, 10:30:58 PM »
Quote
So I added the capacitors again and when I connected the coil it blew both transistors and the fuse.
Such events are always frustrating. :(
Did you check the TVS diodes?  Sometimes a TVS diode will fail first, causing IGBTs to then fail.

Quote
They were my last two 60N65SMD.
Now I'm doing tests with IRFP460.
FETs and IGBTs are significantly different is several ways.  Not too surprising that behavior changed.

Quote
Some photos of how the coil looked:
Nice photos.  Helps to see details.

Shielding between coil and electronics is a good idea.  That shield is close enough to primary and bottom of secondary to change inductance and coupling and loss a bit.  Would require modeling and/or testing to see how much.  My rule-of-thumb is to have primary radius (half of primary diameter) of space between coil and shield to avoid such affects.  Closer may be OK if tuning matches reduced inductances and coupling factor.

With no ground planes and with control circuitry not far from power circuitry, there are many possibilities for unwanted feedback and noise.  One patch might help with the power section of your existing ECB:  There is a large loop in the power supply from low-side emitter to high-side collector.  Adding capacitor(s) directly from low-side emitter to high-side collector would provide a more direct path for the high frequency switching current in that path.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #37 on: November 29, 2023, 08:12:27 PM »
Well, I did some more tests and discovered a few things.
The reason the output was very weak was due to the duty cycle potentiometer wire being broken and hidden under the insulation. However, I only discovered this because I checked the duty cycle time on the oscilloscope and realized that even at 20k it was no more than 10ms.
I switched to this potentiometer for a 50k one and now the output without the resonant capacitors is back to normal.

Despite having "solved" this problem, I wanted to understand what happened.

Now what I'm trying to solve is the fact that when I use resonant capacitors the coil has no output and just lights up a neon lamp.
I removed the TVS just in case, but the behavior didn't change.

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #38 on: November 30, 2023, 05:34:32 AM »
Quote
Now what I'm trying to solve is the fact that when I use resonant capacitors the coil has no output and just lights up a neon lamp.
Can't think of anything useful to say without seeing scope captures.
David Knierim

Offline TiagoBS

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Re: Feedback current transformer doesn't work
« Reply #39 on: November 30, 2023, 07:38:21 PM »
I did some more tests and it seems like I'm narrowing down the possibilities.

1 - When I touch the probe to pin 3 of the 555 on the left, it seems that the duty cycle is reduced and the coil stops having output and just lights up a small neon lamp. (without resonant capacitor)

2 - You can see the duty cycle being adjusted when I test pin 5 of the 555 on the left. Another point is that it is only possible to notice this change in the duty cycle after the potentiometer is turned around 60%.
However, you can see and hear the difference in output throughout all the potentiometer adjustment.(without resonant capacitor)
-

-



3 - Touching the probe to any of the Mosfet Gates causes the duty cycle to increase again. (without resonant capacitor)
[Video]

4 - Adding the resonant capacitor to the primary and measuring pin 3 of the 555 on the left, it is possible to notice that the duty cycle varies between 500us and 750us. This change is possible to notice by turning the 20k potentiometer (now 50k) but only during the first 15% of possible regulation, after that the cuty cycle remains close to 750us for the rest of the potentiometer adjustment.

Apparently I have problems with my osiloscope and that's why I'm using this portable one.
Using this other oscilloscope I didn't notice that much noise and it's even possible to see the ramps.
-





Perhaps some component of the switch is having problems?
« Last Edit: November 30, 2023, 07:40:11 PM by TiagoBS »

Offline davekni

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Re: Feedback current transformer doesn't work
« Reply #40 on: November 30, 2023, 10:02:33 PM »
Quote
2 - You can see the duty cycle being adjusted when I test pin 5 of the 555 on the left. Another point is that it is only possible to notice this change in the duty cycle after the potentiometer is turned around 60%.
Something's wrong if you see a signal on pin 5.  That is internal 2/3rds of supply reference byapssed to ground with a 0.1uF capacitor.

Quote
1 - When I touch the probe to pin 3 of the 555 on the left, it seems that the duty cycle is reduced and the coil stops having output and just lights up a small neon lamp. (without resonant capacitor)
3 - Touching the probe to any of the Mosfet Gates causes the duty cycle to increase again. (without resonant capacitor)
[Video]
Obviously there are significant issues with circuit sensitivity and noise to be so sensitive to scope probing.  Will probably be difficult to obtain reliable predictable operation without designing a circuit board with ground plane.

David Knierim


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Re: Feedback current transformer doesn't work
« Reply #41 on: December 12, 2023, 09:40:52 PM »

 


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post Re: First DRSSTC, Full Bridge PCB & IGBT Selection question.
[Dual Resonant Solid State Tesla coils (DRSSTC)]
davekni
November 19, 2024, 05:31:47 AM
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[Dual Resonant Solid State Tesla coils (DRSSTC)]
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November 19, 2024, 02:33:42 AM
post Re: Testing and teardown of a commercial induction heater
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dejuli2
November 18, 2024, 11:19:28 PM
post Re: First DRSSTC, Full Bridge PCB & IGBT Selection question.
[Dual Resonant Solid State Tesla coils (DRSSTC)]
Benjamin Lockhart
November 18, 2024, 08:43:20 PM
post Re: Testing and teardown of a commercial induction heater
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DashApple
November 18, 2024, 06:07:11 PM
post Re: Is intentional overlap in the secondary theoretically possible?
[Dual Resonant Solid State Tesla coils (DRSSTC)]
MinuteMylar
November 18, 2024, 05:04:09 PM
post Re: First DRSSTC, Full Bridge PCB & IGBT Selection question.
[Dual Resonant Solid State Tesla coils (DRSSTC)]
Beggernator.
November 18, 2024, 12:17:41 PM
post Re: Testing and teardown of a commercial induction heater
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dejuli2
November 18, 2024, 09:25:38 AM
post Re: First DRSSTC, Full Bridge PCB & IGBT Selection question.
[Dual Resonant Solid State Tesla coils (DRSSTC)]
davekni
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