Author Topic: CM400 Induction Heater  (Read 4996 times)

Offline markus

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CM400 Induction Heater
« on: March 02, 2024, 06:46:15 PM »
Hi all,

by chance I got the opportunity to take over a half-finished induction heating project from a nearby school. Their main goal was to melt metal and pour some stuff, for example metal parts for other projects. They could not find anyone to continue the project however, and so it has been sitting around for some time now.
Since I already experimented with induction heating - a self-built heater based on Marko's royer design managing about 800-1000W - and always wanted to build something bigger, this seemed like the perfect opportunity.

From the school project I got a bunch of mostly separate parts, mainly the following:
  • Mitsubishi CM400DU-12F full bridge
  • 3 IXYS IXIDM1401_1505_O isolated integrated driver modules. Each contains two isolated gate drivers with 10 A gate current, 15 V positive and –5 V negative gate voltage. They have some nice features like short-circuit protection, active clamping, UVLO and built-in dead time delay.
  • 4x B43586-S4338-Q4 Epcos caps rated at 3300uF / 350V (should be good for at least 25Arms each)
  • 2x 1uF 1kV MKP snubbers (apparently they got those as a freebie with some other parts - nobody knew what they were supposed to be used for, so they did not find their way onto the project so far)
  • 90x Wima FPK1 0.22uF 400V DC / 250V AC ±5% caps in 3 banks with 3D-printed enclosure
  • 3 6mm work coils: 1x 7 turns 5cm ID, 2x 5 turns 9-10cm ID
  • A graphite crucible setup with isolation
  • radiator etc for water cooling
  • 3 12V 123A server PSUs
  • some copper / bus bar pieces
  • also a chinese ZVS induction heater board from an earlier stage of experimenting

If needed, I can also order more parts via the school (it still somewhat counts as a school project).




The project did not include a driver or anything similar yet. The plan was apparently a simple series LCR that would be driven at a fixed frequency, without feedback or power control.

It seems like various changes are needed to arrive at a nice high-powered result, and I have a rough idea of where to go after going through the forums and looking at other projects.

For now, I did a bit of a cleanup on the setup and added the snubbers and some bleeder resistors. Then I connected everything as series LCR and ran some low power tests using my UD+ with GDTs etc, together with a simple interrupter with no duty cycle limit. The MMC currently consists of 60 Wima caps for 13.2uF total.


At 15% duty cycle it pulls 20A / 12V, and slowly heats up the object. The resonant frequency is 31kHz. After a few minutes the heat sink and the black wires were slightly warm, the rest stayed cold to the touch.

Here scope shots from the test run:


Unfortunately it seems like my gate drive cannot do CW operation - at 40% duty cycle the gate resistors get pretty hot already, even though right now I have two in parallel (2W 5.6Ohm each). I tried removing the TVS since some people reported similar issues resulting from their added capacitance, but could not perceive any improvement.



Here my gate waveforms (could be slightly faster, but currently I do not have smaller gate resistors available):



What do you think is the best way to use these parts? Here some of my thoughts and questions so far:

  • Any tips for how I can achieve CW operation without melting my gate resistors? So far this is the most pressing issue for me. Is it normal that they get that hot?
    Could the long wires be an issue (I did not cut them since they are supposed to go into my DRSSTC project), would lowering the gate resistance be enough, or maybe lowering the voltage to something like 15V?
    If nothing helps, I might switch to the IXYS gate driver modules. I think I should be able to route the FPGA output signals to the driver modules instead of the onboard driver stage. What seems annoying though is that the driver modules expects 15V, which means I have to make some changes on the UD+. Also it has a derived 3.3V supply for a controller which is supposed to make things simpler, but since the UD+ has its own 3.3V supply, I apparently have to deactivate that and feed the driver with my own supply instead (observing some startup and shutdown sequences).
  • As for power control / current limiting, I was thinking about using the DRSSTC driver features and go with the UD+ builtin freewheeling / pulse skipping. Do you see any issues with that?
  • How far do you think I can push the Wima MMC? Right now with 60p = 13.2uF the MMC is rated for 168Arms. I will keep within the 250V AC rating as long as I do not cross 600A, and frequency-dependent datasheet AC voltage rating (80V-ish at 30kHz) while staying below 200A. Downside of the large capacity is that it makes current regulation more difficult, I am also aware that I might have to rebuild it for better cooling once things start to become hot.
    Also, would a different MMC configuration be better (lower capacity / higher voltage)? I can source more Wima caps from the school if needed.
  • To achieve real power I will have to add some method of impedance matching, though for now I want to get the gate drive working first. I have been going through the forums reading up on LCLR / transformer coupled topologies, and right now I think of going for transformer coupled. Not only does it provide galvanic isolation, if my understanding is correct the UD+ is also not suited to drive LCLR, since I would have to stay slightly above the resonant frequency with that topology.

I hope I can build something nice and have lots of fun with this project.

Thanks a lot for you feedback!

Edit: Btw is it possible to resize images in my post so that they take less space?
« Last Edit: March 02, 2024, 06:53:40 PM by markus »

Offline davekni

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Re: CM400 Induction Heater
« Reply #1 on: March 02, 2024, 10:19:09 PM »
Quote
I tried removing the TVS since some people reported similar issues resulting from their added capacitance, but could not perceive any improvement.
These ~600W TVS diodes typically have ~1nF capacitance, insignificant compared to Cge.

Quote
Any tips for how I can achieve CW operation without melting my gate resistors? So far this is the most pressing issue for me. Is it normal that they get that hot?
Could the long wires be an issue (I did not cut them since they are supposed to go into my DRSSTC project), would lowering the gate resistance be enough, or maybe lowering the voltage to something like 15V?
Driving a brick CW requires a lot of gate power.  Yes, hot resistors is normal.
Lowering to +-15V will help by (15/20)^2, cutting power almost in half.  Even at +-15V, there is ~4.6W to dissipate (5uC * 30V * 31kHz).  Lower resistance does not change that 4.6W total.  If low enough, will push some of that power back into UD+ output FETs.  And 2.8 ohms is already under spec'ed minimum external resistance of 3.1 ohms.  Likely doesn't matter for low bus voltage.
Long wires (high GDT leakage inductance) increases gate power only if high enough to cause Vge overshoot.  Scope waveforms show no issue there.

I'd suggest lowering to +-15V and accepting 4.6W (using more or larger resistors).  Another option is to reduce to +15/-0V (or +20/-0V) with something like this circuit on GDT secondaries:
    https://highvoltageforum.net/index.php?topic=2389.msg17547#msg17547

Quote
How far do you think I can push the Wima MMC? Right now with 60p = 13.2uF the MMC is rated for 168Arms.
Since this isn't going to run 24/7, I'd push caps.  Might get away with 2x RMS rating if caps are spaced out a bit for air flow and fans added.

Quote
Downside of the large capacity is that it makes current regulation more difficult
Why is current regulation more difficult?

David Knierim

Offline markus

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Re: CM400 Induction Heater
« Reply #2 on: March 03, 2024, 08:57:27 AM »
Thanks for your reply!

I will mod my UD+ so it can run from 15V and get some beefier gate resistors.

Your GDT buffer circuit looks nice, but if needed I will try to get the IXYS gate drivers to work since I already have them. The nice thing with these is that they run from a single 15V supply and derive their isolated supplies themselves. I will keep it in mind though for future projects!

Quote
Why is current regulation more difficult?
I meant that with large tank capacitor current ringup will be very fast, making it harder to precisely set your desired current limit with an OCD (kinda like a super low impedance DRSSTC). It might not matter that much since we do not go for extreme currents anyways.

Offline davekni

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Re: CM400 Induction Heater
« Reply #3 on: March 03, 2024, 08:01:42 PM »
Quote
Your GDT buffer circuit looks nice, but if needed I will try to get the IXYS gate drivers to work since I already have them. The nice thing with these is that they run from a single 15V supply and derive their isolated supplies themselves. I will keep it in mind though for future projects!
The IXYS gate drivers should work well.  My GDT buffer does not require any external power.  Vge rising edge is provided by GDT secondary.  No buffering on rising edge.  Falling edge is pulled to 0V with local FET.  Requires no extra power supply.  Makes falling edge faster and limits Vge to 0V rather than negative.  Latter change reduces required gate drive power due to 0V minimum.  Theoretically to 25% (down by 75%), but about 30% in practice.  Even though unbuffered, rising edges are a bit faster because other GDT secondary windings (ones turning off) are only lightly loaded.

Quote
I meant that with large tank capacitor current ringup will be very fast, making it harder to precisely set your desired current limit with an OCD (kinda like a super low impedance DRSSTC). It might not matter that much since we do not go for extreme currents anyways.
Thank you for the explanation.  Makes sense.

Good luck with your project.
David Knierim

Offline Mads Barnkob

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Re: CM400 Induction Heater
« Reply #4 on: March 03, 2024, 08:02:48 PM »
Not a bad project to restart, good parts all around and not a huge rat nest :)

Water reservoir is however too small, even with a radiator, a good old floor bucket can sustain some run times of like 15 minutes and its up to bathing temperatures. Reuse of cooling water is then possible in the shower ;)

There certainly is something "off" with the high capacity. I think you are looking at some unfavorable Q factors.

That MMC will also burn to the ground. You do mention that you need to cool it better, but I call for a total reconstruction.

You should have space between each individual capacitor, in both directions. Best way to achieve a MMC that can be cooled is to use small cuts of copper or brass plate/band to solder them together with. Film capacitors get rid of their heat from 2/3 through the leads and 1/3 through the package. The small copper/brass plates will work as heat sinks and with space between all caps, forced air cooling can flow between them.



I would also not trust that distance between the high voltage side (between L and C in resonant circuit), even worse if you go up in current with a small capacitance MMC.



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Offline markus

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Re: CM400 Induction Heater
« Reply #5 on: March 06, 2024, 03:34:55 PM »
Good point about the isolation distance! I bent the leads apart from each other just in case.
The current setup is mostly just to get a feel for how everything works anyways and to experiment with stuff like current limiting, or different MMC capacity.
For proper operation I plan to completely reconstruct the MMC anyway to something water-cooled (what I meant with "better cooling").
But I plan to do that at the same time as I am setting up a proper water-cooled tank circuit, together with a transformer for impedance matching.

Quote
There certainly is something "off" with the high capacity. I think you are looking at some unfavorable Q factors.
Yeah, current rises pretty fast even at 12V.  Actually the original project had an even higher capacity (19.8uF), I already removed one of the cap bank modules.
So does this mean I would be better of with a lower capacity, for example half? A quick test shows that I end up around 40kHz with that.
Downside is that my Arms will also be cut in half...  The unfortunate thing is that even though they are free, this specific choice of caps makes building a properly dimensioned MMC a bit awkward. Either I end up with high Arms but high capacity, or with more reasonable (?) capacity and low Arms. For smaller MMCs the voltage rating also starts to become a problem.
This means I will have to go with a series combination to keep current Arms, but that makes the build more troublesome.

Meanwhile I did more tests with one of the 123A 12V PSUs, and got some usable results already!
Depending on the load, tank current ranges from 200A to 350A, after reaching the curie point the current grows in excess of 400A. The current setup is too weak however to do much heating beyond the curie point. Right now current limiting is set to ~360A (using freewheeling), which should still be fairly safe for the IGBTs I assume.
At 50%-ish duty cycle I approach 1.5kW input power, which is the limit of my variac (I plug the PSU in there because it has nice voltage / current meters).

MMC stays pretty much cold to the touch so far, but the IGBT heatsink started heating up so I added a bunch of fans for cooling, which should also provide a bit of airflow to the MMC. I also added a water bucket for cooling the work coil.
The bus caps are only rated for 30A at most, so I added the remaining two to get 13.2mF at 120A rating. At 1.5kW input power I should have some >100A current (my 10mm2 wiring to the PSU gets pretty warm already), and since I do power control via PWM (using the interrupter), I assume the caps should see a fair bit of stress.
Btw - is it better to connect one of the supply wires to the other end of the "U" instead for better current sharing between the bus caps? Or is this a bad idea since I will get a huge loop = adding lots of inductance? Would it be an issue for the PSU if I completely removed the bus caps (since I am using an interrupter)?

Here the current setup:


And here some waveforms. First with medium load and the second shows current limiting with freewheeling:


Next I plan on doing some tests with higher duty cycles, some 24V tests, and different MMC sizes.
Then I will try to convince the school I need material for upgrades to tank circuit / MMC, and impedance matching.


edit: I forgot to mention that switching to 15V really improved the temperature of the gate resistors. They still get kinda hot with higher duty cycles, but the larger resistors I ordered will help with that hopefully.
« Last Edit: March 06, 2024, 07:10:21 PM by markus »

Offline davekni

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Re: CM400 Induction Heater
« Reply #6 on: March 07, 2024, 01:19:03 AM »
Quote
So does this mean I would be better of with a lower capacity, for example half? A quick test shows that I end up around 40kHz with that.
Downside is that my Arms will also be cut in half..
Higher frequency generally requires less current to deliver same power to load being heated.  However, that depends on load.  And you can easily increase current by supplying higher bus voltage.  Especially for experimenting before adding impedance matching, higher frequency will be closer to reasonable impedance.

Quote
edit: I forgot to mention that switching to 15V really improved the temperature of the gate resistors. They still get kinda hot with higher duty cycles, but the larger resistors I ordered will help with that hopefully.
Higher frequency increase gate resistor power proportionately.  That is one down-side.  But gate power resistors are relatively inexpensive.  Or change to a buffered circuit.

Quote
IGBT heatsink started heating up
Expected.  Switching losses are low with ZCS and low bus voltage.  Vce forward drop is the dominant loss, tracking current, not voltage.

Quote
Btw - is it better to connect one of the supply wires to the other end of the "U" instead for better current sharing between the bus caps? Or is this a bad idea since I will get a huge loop = adding lots of inductance?
Unlikely to make any significant difference.  Most AC (ripple) current is between IGBTs and caps.  Inductance to supply is not very important.

Quote
Would it be an issue for the PSU if I completely removed the bus caps (since I am using an interrupter)?
Probably would be a problem.  Most PSU output capacitors are intended to handle ripple current generated within PSU, not huge ripple current from load.
David Knierim

Offline petespaco

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Re: CM400 Induction Heater
« Reply #7 on: March 07, 2024, 04:32:17 AM »
Just being a curious bystander-----

I don't understand why the tank current would rise "after the temperature reaches the curie point".  What ferrous metals are you heating at that time?
In my humble (ZVS  induction heating) experience, current DECREASES as ferrous metals in the work coil reach the curie point.

I notice a graphite crucible sitting beside the work coil in one picture, but that isn't ferrous, so "curie point" wouldn't apply.  Right?

Do I understand that your input voltage to the IGBT's is only 12 VDC for all these tests?  Why not more?

Pete Stanaitis
---------------


Offline davekni

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Re: CM400 Induction Heater
« Reply #8 on: March 07, 2024, 05:12:31 AM »
Quote
I don't understand why the tank current would rise "after the temperature reaches the curie point".  What ferrous metals are you heating at that time?
In my humble (ZVS  induction heating) experience, current DECREASES as ferrous metals in the work coil reach the curie point.
Yes, same load change at Curie point causes opposite power change.  ZVS drive (parallel drive resulting in fixed voltage across coil) consumes less power when load Q increases.  H-bridge drive in series with coil consumes more power when load Q increases.

Quote
I notice a graphite crucible sitting beside the work coil in one picture, but that isn't ferrous, so "curie point" wouldn't apply.  Right?
I was wondering the same thing.  Depends on crucible electrical conductivity and geometry and drive frequency.  Test may or may not have included crucible, at least I didn't notice that being specified.  If crucible was included, implies it's conductivity is too low to block most magnetic field from center.  Higher frequency (resulting in higher volts/turn for same magnetic field) will move more heating to crucible and away from iron in center.
David Knierim

Offline markus

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Re: CM400 Induction Heater
« Reply #9 on: March 07, 2024, 05:07:37 PM »
Thanks for your replies dave, they are very helpful!

Quote
Higher frequency generally requires less current to deliver same power to load being heated.  However, that depends on load.  And you can easily increase current by supplying higher bus voltage.  Especially for experimenting before adding impedance matching, higher frequency will be closer to reasonable impedance.
That is good to know, I will experiment with that a bit more. My main concern however was the current rating of the MMC, since less parallel caps = less current rating. Halfing the capacity would drop the MMC Arms rating from 168A to 84A, which seems to be kinda low - even more so with lower capacities.


Quote
I don't understand why the tank current would rise "after the temperature reaches the curie point".  What ferrous metals are you heating at that time?
In my humble (ZVS  induction heating) experience, current DECREASES as ferrous metals in the work coil reach the curie point.
My setup is pretty much the same as a DRSSTC (with super low impedance), with the work piece in place of the secondary. As long as I feed the tank with energy, I will get high current ringup. Meanwhile the workpiece acts as a load and takes energy out of the system. Higher load removes more energy = less current in the tank.

Quote
    I notice a graphite crucible sitting beside the work coil in one picture, but that isn't ferrous, so "curie point" wouldn't apply.  Right?
The mentioned tests were with some random piece of metal - a ball bearing, a fat bolt, a piece of iron pipe. The large crucible is too big to fit into this work coil, I would have to switch coils for testing. Since the point of the school project was to melt metals, the crucible will certainly see some use. It is sitting there because I wanted to try if it would not perhaps fit in by chance, but it touches the coil in multiple places.
I gave the smaller crucible a try though (empty), and it presents a very light load. At 12V / 50% duty cycle it takes ages to heat up and only gets to the point where it is glowing a bit.

Quote
Do I understand that your input voltage to the IGBT's is only 12 VDC for all these tests?  Why not more?
Yes, all tests were on 12V input. I will do 24V tests next - I already prepared two stacked 12V PSUs for that which you can see in the last picture - but I expect very fast current ringup, which might make current limiting a bit difficult. So I might have to play with lower MMC size and higher frequencies.



Meanwhile I managed to track down an issue that has been plaguing me during the last few days:
My driver would sometimes skip interrupter pulses while signalling some fault / ocd, and sometimes even lock up completely. I could track this down to cases with high load.
It seems that with high load, there is (almost) no current during the first half cycle, meaning feedback starts only in the second half cycle. The UD+ compares this with the startup oscillator and since the second half cycle is negative, it thinks the frequency is way too low. Therefore it raises a feedback error and disables the output for the rest of the interrupter pulse.
Here some scope shots, first normal operation and the second showing the issue. Pink is the OCD / fault output, blue the cleaned up feedback signal. Startup oscillator is set to 3 cycles for debugging, normally I use 1 (I probably do not need it at all):



I thought I would have to reduce the number of turns on the feedback / OCD transformers (careful not to blow up the burden resistor with CW operation), or modify the VHDL to skip the feedback check during the first half cycle.
But while writing this I figured I could also swap GDT output and feedback polarity, so the second half cycle turns out positive instead of negative. This would be the easiest solution, but probably the issue will come back to bite me once I forget about it in the future ;D
« Last Edit: March 07, 2024, 05:21:03 PM by markus »

Offline davekni

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Re: CM400 Induction Heater
« Reply #10 on: March 07, 2024, 10:46:42 PM »
Quote
Meanwhile I managed to track down an issue that has been plaguing me during the last few days:
Looks like you need a bleed resistor across H-bridge output.  That way startup will be consistent.  Without resistor, leakage current of IGBTs defines initial bridge output voltage.  If output happens to be at same level as first half-cycle drives it, no current is generated.
Yet faster startup can be achieved if two resistors are used to bias initial H-bridge output to either + or - Vbus.  However, that requires checking which polarity first half-cycle drives H-bridge, then adding resistors to bias output to opposite polarity.

Quote
I gave the smaller crucible a try though (empty), and it presents a very light load. At 12V / 50% duty cycle it takes ages to heat up and only gets to the point where it is glowing a bit.
Any non-magnetic load is likely to be less effective (higher Q), so require higher voltage (higher current and/or higher frequency).
David Knierim

Offline petespaco

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Re: CM400 Induction Heater
« Reply #11 on: March 08, 2024, 01:59:43 AM »
Quote
I gave the smaller crucible a try though (empty), and it presents a very light load. At 12V / 50% duty cycle it takes ages to heat up and only gets to the point where it is glowing a bit.
Pardon my butting in on this thread since I have such limited experience.
But---   
With my 2500 watt Chinese induction heater running on 48 volts (at, I'd say, 100% duty cycle)  I'd draw about 35 power supply amps with a crucible of about that size in the work coil..  Subtract about 5 amps for what I call "idle current",   and I have about 30 X 48 = 1440 watts going into the crucible.  Within a couple of minutes, it starts to glow and within 10 minutes it is glowing a very bright orange, even with a couple of hundred grams of copper scrap in it.
So----  you are at about 1/4 of that input voltage and only half the "on time", for about 180 net watts into the work,  so I am not surprised that you don't see much heating going on.  If I were you, I'd get that supply voltage up as much as you can.

What is your goal for melting metals?
-Ferrous?  Non-Ferrous?
-Weight?   100 grams?  1000 grams? 
-Melt time to pouring temp?   I minute?  1 Hour?

Are you measuring power supply input current?  I'd suggest that you do that so you can get an idea of overall circuit efficiency.

Offline markus

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Re: CM400 Induction Heater
« Reply #12 on: March 25, 2024, 02:06:41 PM »
Thanks for your replies everyone! I kinda forgot to post, but did make progress in the meantime.


Quote
What is your goal for melting metals?
-Ferrous?  Non-Ferrous?
-Weight?   100 grams?  1000 grams?
-Melt time to pouring temp?   I minute?  1 Hour?

Thanks for your input and the numbers! What we plan on melting:
  • Various aluminium parts - my friend wants to try and pour metal parts for his projects. For now at most a few hundred grams I think, using a graphite crucible.
  • My sister and me will be doing comparatively small stuff with high level of detail, for example jewelry and ornaments. So aluminium, silver, steel, maybe even gold. My sister does a lot modelling and pouring in a dental lab, so we have professional expertise on hand. She is pretty hyped about the project, and even managed to get a bunch of used small graphite and ceramic crucibles from the lab. Of course she also found various issues with our primitive / naive methods  ;D (her usual requirements are of course perfect quality in all aspects, but she is willing to make some compromises).
  • Since my sister works with steel a lot, being able to melt steel would definitely be nice as well.
  • And of course melting some random stuff for fun.

For the melting time I think something like 10-ish from the top of my head. However this will probably be skewed by the fact that my sister wants to preheat the filled crucible, and of course the form too. Edit: Apparently only steel is preheated


Quote
Any non-magnetic load is likely to be less effective (higher Q), so require higher voltage (higher current and/or higher frequency).
I'm trying to wrap my head around why higher frequency is more effective on nonmagnetic loads where we do not have hysteresis losses - is it because higher frequency leads to a higher voltage across the work coil?



Quote
Looks like you need a bleed resistor across H-bridge output.  That way startup will be consistent.  Without resistor, leakage current of IGBTs defines initial bridge output voltage.  If output happens to be at same level as first half-cycle drives it, no current is generated.
Thanks for the tip! I added a 220R 15W resistor and with that the issue is gone. I cannot believe I forgot about that since I definitely remember reading about that kind of issue before on the forums.

As for other changes, I upped the input voltage to 24V and then 36V and changed the MMC from 13.2 uF (1s60p) to 3.3 uF (2s30p), increasing the frequency to about 66kHz with the small coil.
With this, I now get 2-2.5kW input power. I can measure input current on the 36V output with the help of my multimeter which has a current clamp.
I also replaced the gate resistors with 2x 3W and added a fan, with that gate resistors are ok even in CW mode at 66kHz.

I now get some pretty nice heating on all kinds of scrap metal, with the pieces that have good coupling reaching the melting point (pipes etc). Smaller stuff only glows orange at most.
Here's a 2.5cm iron pipe and a ball bearing:


With this I also get my crucibles to heat up nicely and can melt aluminium. However since I only have a temporary setup, MMC and IGBTs start to overheat after some time, which forces me to abort. Pretty sure the heat sink is just too small for 300-400A. Meanwhile on the MMC the new setup leaves me with just 3 wires in parallel, which is just too little copper area - so the wires heat up even though the caps themselves would remain cold.


With all the experimenting on the current setup and a bunch of reading, I feel that my understanding of the system has improved a lot. Since the temporary set up has reached its limits, it is time to start with the real setup. My goal is to reach 10kW if possible.
  • For the matching transformer I found some 80/40/15 ferrite rings made from K4000 material that I plan to buy (https://www.kaschke.de/wp-content/uploads/2017/06/K4000.pdf). 8 of these should give me enough cross section to not saturate even at a worst case of 565V / 8 turns / 20kHz. Before I actually buy them, do you see any issues with these cores? For example the material being wrong, or the inner diameter being too small etc.
  • For the DC blocking cap I plan on getting a number of small MKP DC-Link caps (B32676E3126K) for about 200uF and >= 100Arms rating. They are rated for 300Vdc, but that should not be an issue since they will only see a few volt at >20kHz.
  • For winding the matching transformer I have 0.5mm diameter magnet wire (liberated from an old TV) which I will use to create makeshift litz wire. This should be just right given a skin depth of 0.26mm at 60kHz. I just hope I have enough...
  • I plan on running the inverter from rectified 230V. Full wave rectified 3 phase would be better, but the IGBT modules are only rated for 600V, with is way too close to the 565V they would see. Perhaps I will replace them with some smaller 1200V modules I have lying around.
  • Of course I will also redo the tank circuit so everything is water cooled, including MMC and the secondary of the impedance matching transformer.
    I plan to use either 12mm stiff (MMC) or 8mm soft copper pipe (matching transformer secondary - a leftover from my DRSSTC), but need to find some suitable fittings for connecting everything together.
    I will add some more caps in parallel to the MMC so I can get a higher Irms rating and reduce the voltage across the tank capacitor - from 2s30p with 3.3uF now to at least 2s60p for 6.6 uF at 800V DC / 500V AC rating. This will drop the resonant frequency with the small coil from 66kHz to less than 50kHz.
    Or I could use all the caps and go for 3s60p, resulting in 4.84uF at 1200V DC / 750V AC for a better voltage rating.
« Last Edit: March 26, 2024, 12:08:39 PM by markus »

Offline Anders Mikkelsen

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Re: CM400 Induction Heater
« Reply #13 on: March 25, 2024, 04:47:17 PM »
Congratulations on getting it working. As you've seen, not having a matching transformer leads to a lot of losses in the IGBTs, given that it restricts you to using a pretty low bus voltage in order to keep the power at a reasonable level. This will be even less favorable with more difficult loads, since the series resonant tank will draw maximum current when the loading is the lightest (highest Q), while a ferromagnetic steel tube will present the lowest Q of any practical load.

Your IGBTs are also pretty oversized in terms of rated current. I would aim for some more modern 1200 V parts of lower rated current, and operate it off rectified 3-phase mains. A full bridge running from 560 V bus would only need to push some 25 - 30 A to deliver your target power, so using 400 A parts just leads to uneccessary drive power requirements.

For the matching transformer, 0.5 mm wire is technically within a few skin depths of the operating frequency, but as long as you have more than a single wire then you also need to consider proximity effect. For this frequency, I would go with 0.1 mm or finer litz, but 0.2 mm is likely also fine, especially if you use a single layer winding on your toroid.

The ferrite should work fine. At these low frequencies, any power grade of ferrite should be fine.

Your caps are rated at 2.5 A RMS a piece for 15 degree internal heating. If we aim for the best practical external cooling, we can get away with 60 degrees heating, so double the current, that's 5 A per cap. .22 uF is 15 ohms at 50 kHz, which gives you a cap voltage of 15*5 = 75 V RMS at the maximum rated cap current, or 5 A * 75 V = 375 VA per cap, for a total of 34 kVAR for the 90 caps, independently of how they are configured. Right now it also looks like you have some stray inductance in your tank circuit which will eat up some of those VARs as well, by the ratio of work coil inductance to total tank inductance.

With a steel tube in the coil, you might end up with a Q as low as 4, which allows you to transfer 34/4 = 8.5 kW while staying within the ratings of your capacitors. For solid steel well matched to the size of the coil, Q might be 5 - 8, up to a few times that for smaller work pieces. For aluminium workpieces, a Q in the 20 - 50 range is not unrealistic, and for copper it can exceed 100. It follows that the power throughput will be very limited. I would definitely look for a larger capacitor if you're aiming for 10 kW. I would aim for at least 300 kVAR for a heater of this size, to give some leeway for processing a usable fraction of the rated power across a range of loads. Where are you located? A proper induction heating cap doesn't need to be particularly expensive.


Offline davekni

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Re: CM400 Induction Heater
« Reply #14 on: March 26, 2024, 04:00:43 AM »
Quote
I'm trying to wrap my head around why higher frequency is more effective on nonmagnetic loads where we do not have hysteresis losses - is it because higher frequency leads to a higher voltage across the work coil?
Yes, higher work coil voltage, which translates to higher volts/turn at load too.

Quote
With a steel tube in the coil, you might end up with a Q as low as 4, which allows you to transfer 34/4 = 8.5 kW while staying within the ratings of your capacitors. For solid steel well matched to the size of the coil, Q might be 5 - 8, up to a few times that for smaller work pieces. For aluminium workpieces, a Q in the 20 - 50 range is not unrealistic, and for copper it can exceed 100.
Anders:  Any idea what Q range would be for graphite crucibles?  I'd expect Q to be well lower than for directly heating copper or aluminum.  If I understand correctly, Markus' plan is to use graphite crucibles for melting.
David Knierim

Offline Anders Mikkelsen

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Re: CM400 Induction Heater
« Reply #15 on: March 26, 2024, 01:41:49 PM »
Quote
I'm trying to wrap my head around why higher frequency is more effective on nonmagnetic loads where we do not have hysteresis losses - is it because higher frequency leads to a higher voltage across the work coil?
Yes, higher work coil voltage, which translates to higher volts/turn at load too.

Quote
With a steel tube in the coil, you might end up with a Q as low as 4, which allows you to transfer 34/4 = 8.5 kW while staying within the ratings of your capacitors. For solid steel well matched to the size of the coil, Q might be 5 - 8, up to a few times that for smaller work pieces. For aluminium workpieces, a Q in the 20 - 50 range is not unrealistic, and for copper it can exceed 100.
Anders:  Any idea what Q range would be for graphite crucibles?  I'd expect Q to be well lower than for directly heating copper or aluminum.  If I understand correctly, Markus' plan is to use graphite crucibles for melting.

I just did some quick measurements with a tight fitting coil around a large crucible, the best practical case, and it goes from around 3.5 at 30 kHz to 5.5 at 100 kHz, so not too bad. This is practically with no clearance between the coil and crucible, so I would target maybe 5 - 8 Q at 50 kHz to give more flexibility in the crucible selection in practice. For a project of this cost and magnitude, I would not skimp on the tank VARs, and the numbers I gave for the FKP1s are really pushing the limit. It's also nice to be able to heat aluminum directly in ceramic crucibles, and steel above the curie point, since my experience is that graphite crucibles oxidize away with time if no protective atmosphere is used. I would still stand by my recommendation to use a purpose-made induction heating cap, given that a 300 kVAR part costs less than 100 euros from normal distributors, and 500 kVAR can be had for less than 150. This gives a lot more VARs per dollar (or euro) compared to FKP1s, with easier mounting, cooling and lower stray inductance to boot. I have  a good stock of new Celem 500 kVAR caps that I got for 25 dollars each, and I would be fine with donating one to the cause if Markus is in Europe, given the cost of shipping here.

Quote
I'm trying to wrap my head around why higher frequency is more effective on nonmagnetic loads where we do not have hysteresis losses - is it because higher frequency leads to a higher voltage across the work coil?
Yes, higher work coil voltage, which translates to higher volts/turn at load too.

Hysteresis loss is not usually very significant, and the large change in Q when steel goes above the curie point is mainly from the drop in permeability. Reflected resistance is proportional to the root of the ratio of resistivity to permeability. Hysteresis loss might represent some 15 - 30 % of losses, but the permeability can easily change from 1000 to 1, giving a loss ratio of sqrt(1000/1) = 30 between being below and above the curie point.

Inductive reactance of the coil, and therefore VARs per amp, rises linearly with frequency. Workpiece deposited power grows with the square root of frequency for a given coil and current, due to the skin depth decreasing with sqrt(F), so you get more heating per amp at higher frequency with a given coil and workpiece, but less heating per VAR. More coil turns gives more heating per amp, while preserving VARs, if the geometry is kept the same, but there's a practical upper limit to how many turns you can have. Since most film caps come with a 500+ V rating, it makes sense to dimension the tank to benefit from that.
« Last Edit: March 26, 2024, 02:37:59 PM by Anders Mikkelsen »

Offline markus

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Re: CM400 Induction Heater
« Reply #16 on: March 27, 2024, 11:53:42 AM »
Hello Anders,
thank you very much for your replies, that is some very useful information there!

You are right about the parts - however, for now I worked with these because I got them for free from this school project (they also got them basically for free from somewhere else).

Quote
Your IGBTs are also pretty oversized in terms of rated current. I would aim for some more modern 1200 V parts of lower rated current, and operate it off rectified 3-phase mains. A full bridge running from 560 V bus would only need to push some 25 - 30 A to deliver your target power, so using 400 A parts just leads to uneccessary drive power requirements.
You are right about the IGBT modules - while drive power is not that much of an issue since I already solved that part, not being able to run from rectified 3-phase mains is not that great. I have quite a number of 150A 1200V BSM150GB120DL IGBT modules sitting around, switching to these would be simple for me.

Quote
Your caps are rated at 2.5 A RMS a piece for 15 degree internal heating. If we aim for the best practical external cooling, we can get away with 60 degrees heating, so double the current, that's 5 A per cap. .22 uF is 15 ohms at 50 kHz, which gives you a cap voltage of 15*5 = 75 V RMS at the maximum rated cap current, or 5 A * 75 V = 375 VA per cap, for a total of 34 kVAR for the 90 caps, independently of how they are configured.
Similar to the IGBTs, I have been using the caps since they were already there from the school project.
That kVAR calculation and the Q numbers were very informative, thank you! Up to now I always found it difficult to figure out just how much power I can / will transfer with a given setup.
Actually, there are 180 caps in total (half of these are still at the school), so I could get 68 kVAR total instead of 34. However that is still rather far away from 300 kVAR unfortunately, so it would probably be best to see if I can get a proper capacitor instead of building a MMC that would be too small anyways. Not to mention the other benefits.
Quote
the numbers I gave for the FKP1s are really pushing the limit.
I have to admit that I already exceed the Irms rating by a lot and pushed the current to 350A for the current 2s30p MMC, even though the caps are only rated for 2.5Ax30 = 75A. This makes for about 90kVAR at 66kHz / 3.3uF. Even so, I did not have the impression that the caps were getting dangerously hot.
Edit: Actually those are peak values, not RMS - so in RMS I this is "only" 250Arms, and only half the VARs for 45kVAR.

But I think you are right about the induction heating caps, and it seems there are some that actually come at an acceptable price (I always had imagined them to be more expensive).
Quote
300 kVAR part costs less than 100 euros from normal distributors, and 500 kVAR can be had for less than 150
What kind of "normal distributors" do you use, or what kind of parts should I be looking for? I only find more expensive prices using mouser / digikey / a search on octopart, with the CDE 300kVAR LC3 series (https://www.cde.com/resources/catalogs/LC3.pdf) at 120-130 EUR/pcs net, and the 500kVAR LC5 series at 270EUR. Only the Dawncap 500kVAR DDC caps (http://www.dawncap.cn/upload/20220423151314.pdf) - a dropin replacement for the Celem C500T - on aliexpress are cheaper at ca. 100EUR/pcs. For celem I could not find a price at all, seems like I would have to request a quote.
However it seems that actually getting one of these is a bit difficult, since most of the CDE are not in stock anywhere and the Dawncap aliexpress store (https://www.aliexpress.com/store/1102804025) seems to sell to every country except for Germany where I live, which is a bummer. No luck on ebay either.

Quote
I have a good stock of new Celem 500 kVAR caps that I got for 25 dollars each, and I would be fine with donating one to the cause if Markus is in Europe, given the cost of shipping here.
Wow, 25 dollars is a great price! Thank you for your offer, I would be very happy about that! I live in germany, I will send you a PN.

Quote
For the matching transformer, 0.5 mm wire is technically within a few skin depths of the operating frequency, but as long as you have more than a single wire then you also need to consider proximity effect. For this frequency, I would go with 0.1 mm or finer litz, but 0.2 mm is likely also fine, especially if you use a single layer winding on your toroid.
I had assumed 0.5mm was fine since this guy in his 60kW induction heater (https://forum.mosfetkiller.de/viewtopic.php?t=64870) used 0.5mm wire (20mm2) and was fine with it. But I can see if I can find something else - I have a one pound reel of 0.12mm (AWG36) and more than a kilogram of 0.3mm wire from my tesla coils, as well as some misc salvaged stuff so there should be something suitable.


Quote
If I understand correctly, Markus' plan is to use graphite crucibles for melting.
Quote
It's also nice to be able to heat aluminum directly in ceramic crucibles, and steel above the curie point, since my experience is that graphite crucibles oxidize away with time if no protective atmosphere is used.
Yes, I will use a graphite crucible, but I also have some small-ish ceramic crucibles I want to use. Being able to melt steel would definitely be nice.
Btw the graphite crucible slowly oxidizing away apparantly also serves as a feature, since this produces a layer of protective gas covering the metal. This seems to be the reason why in the dental lab they use graphite crucibles for stuff like gold instead of ceramic. For materials like iron / steel you cannot use graphite crucibles however, since the carbon will poison the metal.

Meanwhile I also ordered the ferrite cores and caps for DC blocking.
At this rate there will be not much left of the original project when I'm done, just the bus caps, bus bars and work coils :D Oh and of course the extra stuff like the crucible, modelling sand etc.
« Last Edit: March 29, 2024, 03:12:59 PM by markus »

Offline markus

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Re: CM400 Induction Heater
« Reply #17 on: April 09, 2024, 06:08:53 PM »
My setup got some improvements and now runs from 230V AC (single phase)!
I switched the IGBT modules to 150A 1200V BSM150GB120L and added a quickly built matching transformer and a 192uF 300V DC blocking cap. (This means the threat title is now wrong lol)
Matching transformer is 3x R80/40/15 cores with 7 turns of 2p 2.5mm2 I had lying around. At 330V bus voltage and 7 turns the cores will not saturate as long as I stay above 40kHz.
DC blocking cap is 16x B32676E3126K MKP film caps. I noticed later on that these caps are DC link which are made for filtering DC ripple, will I run into problems using these for DC blocking?
Bus caps got reduced back to 2p 3300uF / 350V. For 3 phase operation I will put these in series to get 1650uF / 700V.


IGBTs run much cooler now, matching transformer also remains cool so far. Since the tank cap has not changed, I still stay below 400Apk, but I added more cooling to the MMC.

I think I need to tweak phase lead a bit more, but I need to change the inductor for that.
What is also missing is an inrush current limiter, for now I use the variac for startup.
« Last Edit: April 09, 2024, 06:10:28 PM by markus »

Offline markus

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Re: CM400 Induction Heater
« Reply #18 on: April 30, 2024, 04:54:38 PM »
Hi everyone!

During the last days and weeks I was somewhat busy, but managed to upgrade my setup in various ways.
I got a few successful tests in which I am very satisfied with, but unfortunately shortly afterwards my bridge blew up without clear reason.
Hopefully someone can help me to figure out what went wrong, here the details:

Setup:

Here the current Setup:


Most noticeable is that my project now finally uses a proper Celem cap (C500T 6.3uF 1000kVAR 1000A / 700V, optimal frequency range 26-51kHz). Thank you very much Anders!


The whole tank circuit is now water cooled with 8mm copper pipe, the coil attaches via a set of compression fittings so that it can be swapped when needed. The water cooling setup got upgraded with 8mm tube and a bigger bucket. Btw I found out that I need to be very careful when tightening the fitting, or the compressing ring will refuse to get off afterwards...

In preparation for 3 phase operation I switched the bus cap configuration to 2 3300uF / 350V caps in series giving me 1650uF / 700V, and put a nice three phase rectifier onto my heat sink.


The only important things missing now are inrush current limiting, for which I already procured the necessary materials, and upgrading the matching transformer.


Tests and Failure:

I tested the new setup over two days, running from a 16A 230V single phase input and with a current limit of 600Apk in the tank circuit.

Test was with 7 turns on the matching transformer as before, using a large load (iron pipe, chunk of steel). As it turns out, in the new setup I get much faster / higher current ringup and hit 600Apk very fast, whereas before I would not reach beyond 200-300Apk at most with a large load. Even limited to 16A single phase, the heater seems much more powerful than before and now can get to white hot with ease as you can see in the picture. I popped the breaker however before it started melting, I guess because it got overloaded?
Due to the fast current ringup I rewired the matching transformer for the next tests to get 14 turns (putting the 2 separate windings in series), which is still enough to easily reach 600A. I also redid the phase lead tuning since frequency dropped from 55kHz to 43.5kHz.


The next day I tried melting a small amount of aluminium in a ceramic crucible (with 14 turns on the matching transformer, everything else as before). During testing my pump somehow failed to actually produce water flow, which I noticed when my coil started smoking shortly after I started heating... Luckily it seems nothing got damaged by excessive heat.
The test was very successful and the aluminium melts much faster than before, but after about 2-3 minutes something went pop and the bridge died.
The event was fairly quiet, the pop sound was similar to a contactor or large relay.

I disassembled everything and while bridge is dead with a shorted IGBT module, everything else seems fine. There are also no shorts or melted insulation on matching transformer or the CTs.
I opened up the shorted IGBT module. It seems each IGBT / diode is actually two paralleled pieces internally. Of these paralleled IGBTs one failed for each IGBT, while the diodes look perfectly fine:


Possible causes:

I'm not really sure what could be the cause:
  • At 330V bus voltage I would need some huge voltage spikes to exceed the 1200V rating of my IGBTs. While tuning the phase lead I only saw 150V spikes at most.
  • Similarly, current could hardly be the issue here, since at 600Apk with 14 turns on the matching transformer the 150A IGBTs will only see 43Apk (twice that with 7 turns). The heatsink was pretty cold which also fits.
  • There should be no issues with the matching transformer - at 43.5kHz and 7 turns I get a flux density of 314mT, which still leaves me with a fair amount of head room given a maximum flux density of 380mT for the K4000 material. At the time of failure I used twice the amount of turns, so saturation should be pretty much impossible.
  • What I noticed was that on the bus caps, one screw turned out to be loose (on the connection between the two series caps). There was still contact however, and I do not think that lacking a bus cap would lead to my bridge exploding randomly after a day of testing anyway.
  • I also thought about whether the freewheeling operation overloaded the body diodes - which have a smaller die size than the IGBTs - but the IGBT autopsy showed that is not the case.
  • I also double checked that my GDTs do not saturate at the lowered frequency, even in freewheeling mode.
  • I did notice a strange kind of ringing however, both in normal operation and in freewheeling mode (tested with signal generator / scope). Where does that come from, and is it dangerous? The dip in the middle is not really that deep and looking at the data sheet, the IGBT only starts conducting at 6V so that amount of ringing should not pose much of an issue yet. Nevertheless I want to get rid of it of course, any tips?
  • As I was writing this I remembered that when I was checking gate wave forms sometime earlier, I managed to produce a ground loop from one emitter through my scope lead, popping the breaker (I forgot to remove the scope lead when switching from the isolation transformer to regular mains). I am pretty sure this happened to be the same IGBT that is now shorted, could that have damaged the gate somehow?
  • And last of all, the ebay seller I got these from did not take any measures against ESD and just packed them into refrigerating plastic bags, maybe I was unlucky and the gate got slightly damaged?


I do have replacement parts at hand, but right now I kind of lost trust into my project since I could not figure out a reason for the sudden failure. I fear that after replacing the IGBTs, they will just randomly die again the next day...
Thank you for any thoughts! Hopefully I can figure out how to prevent this from happening again.

Offline petespaco

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Re: CM400 Induction Heater
« Reply #19 on: May 01, 2024, 04:38:56 AM »
One thing that comes to mind:
  Maybe you are getting Fake IGBT's from China.
Over the past few years, I have gotten several fake IRFP260N Mosfets, so if they can cheat on them, why not on IGBT's too?.  I think One guy (on this list?) opened up some of those Mosfets and found that the dies on the fakes he found were only about 1/4 the size of "real" ones.  Now I only buy them from Digikey or Mouser in the USA.
 

Offline markus

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Re: CM400 Induction Heater
« Reply #20 on: May 01, 2024, 09:46:43 AM »
Yes, I've also had fake mosfets from china with a way too small die, after which I bought the real stuff from Mouser. edit: I also remember some mentions of fake IGBT bricks, where the seller somehow replaced the casing and filled in opaque goo instead of the previously clear goo to hide the die. The people were impressed that all this effort was worth the money.

But with the current IGBTs I'm pretty sure that these are just some local guy stripping some inverters or something and making a bit of money. I got a bunch of random 100A, 150A and also some 75A and 200A modules from him that still had the old gate circuitry on them.
Also I've already run the same IGBTs for some (limited) amount of time with the old setup from my previous post (much of the setup including driver also being the same). At 360Apk and 7 turns on the matching transformer this gave me some 50Apk through the IGBTs.
« Last Edit: May 01, 2024, 10:01:48 AM by markus »

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Re: CM400 Induction Heater
« Reply #21 on: May 02, 2024, 05:18:56 AM »
Quote
But with the current IGBTs I'm pretty sure that these are just some local guy stripping some inverters or something and making a bit of money. I got a bunch of random 100A, 150A and also some 75A and 200A modules from him that still had the old gate circuitry on them.
Does sound likely to be genuine given old gate drive circuitry etc.  I have purchased counterfeit IGBTs of TO247 variety from EBay (and gotten refunds after proving data sheet spec's weren't met).  Your situation sounds different enough.

Quote
There should be no issues with the matching transformer - at 43.5kHz and 7 turns I get a flux density of 314mT, which still leaves me with a fair amount of head room given a maximum flux density of 380mT for the K4000 material. At the time of failure I used twice the amount of turns, so saturation should be pretty much impossible.
Probably not, but I don't know enough about UD+ to be certain.  Controlling by secondary current leaves the possibility of sub-harmonic component that builds up excess current due to resonance of primary coupling capacitor set with transformer inductance.  Might be safer to control by primary current.

Quote
What I noticed was that on the bus caps, one screw turned out to be loose (on the connection between the two series caps). There was still contact however, and I do not think that lacking a bus cap would lead to my bridge exploding randomly after a day of testing anyway.
Hard to say when some jarring or magnetically induced force from current may have made momentary disconnects.  I'd inspect that connection for any subtle signs of arcing - black residue or pitting.  Loose power connections are often problematic.

Quote
I did notice a strange kind of ringing however, both in normal operation and in freewheeling mode (tested with signal generator / scope). Where does that come from, and is it dangerous? The dip in the middle is not really that deep and looking at the data sheet, the IGBT only starts conducting at 6V so that amount of ringing should not pose much of an issue yet. Nevertheless I want to get rid of it of course, any tips?
I'm guessing this is Vge ringing.  Not specified.  If so, scope images are needed to make any useful recommendations.

Quote
As I was writing this I remembered that when I was checking gate wave forms sometime earlier, I managed to produce a ground loop from one emitter through my scope lead, popping the breaker (I forgot to remove the scope lead when switching from the isolation transformer to regular mains). I am pretty sure this happened to be the same IGBT that is now shorted, could that have damaged the gate somehow?
This would be first guess as to a cause.  Presuming scope ground was connected to smaller Kelvin emitter pin (pin paired with gate pin), resistance of that path might be high enough to fry something with momentary fault current.  (Second guess is above loose power connection.)
BTW, I made the almost-same mistake once too, forgetting to remove scope ground when switching from isolated to line power.  Wasn't on gate return, so didn't fry anything.  Was a bit surprised that scope and probe both survived too.

Quote
And last of all, the ebay seller I got these from did not take any measures against ESD and just packed them into refrigerating plastic bags, maybe I was unlucky and the gate got slightly damaged?
Poor packaging, but not likely the issue.  I have seen latent failures due to prior partial damage from ESD, but not specifically in IGBTs or power FETs.

Hope your repair and future work goes smoothly.
« Last Edit: May 02, 2024, 06:02:54 AM by davekni »
David Knierim

Offline markus

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Re: CM400 Induction Heater
« Reply #22 on: May 03, 2024, 09:59:22 AM »
Thanks for your input!

Quote
This would be first guess as to a cause.  Presuming scope ground was connected to smaller Kelvin emitter pin (pin paired with gate pin), resistance of that path might be high enough to fry something with momentary fault current.  (Second guess is above loose power connection.)
In that case I will assume that to be the failure cause and rebuild everything. Yes, the scope was connected to the small gate / emitter pins. So far it looks like the scope survived just fine, gotta see if any issues pop up later.

Quote
Controlling by secondary current leaves the possibility of sub-harmonic component that builds up excess current due to resonance of primary coupling capacitor set with transformer inductance.
I think that if the cause would have been overcurrent, the heatsink should have been hot. Still, I will check the primary current during the next run with my scope.
I calculated the resonant frequency of the coupling cap + transformer inductance beforehand, using an estimated inductance of 14,15uH from a similar project (value is for matching transformer with 8 turns and 25cm2 cross section). With 192uF capacity, this gave me a resonant frequency of 3kHz, which is about one order of magnitude away from the expected operating frequency. However while writing this, I noticed that the current matching transformer I put together for testing only has 8.6cm2 cross section, so might have a lower inductance than the estimate. I will check the actual values just to be sure.
I will think about controlling the primary current instead of the secondary. It would have the demerit that I have to readjust the current limit if I change the matching transformer turn ratio and risk exceeding the celem current rating if I forget to do so. But of course with controlling the secondary current, I might exceed the IGBT current rating instead if I am careless.

Quote
I'd inspect that connection for any subtle signs of arcing - black residue or pitting.  Loose power connections are often problematic.
I did check for that, everything looked fine.

Quote
I'm guessing this is Vge ringing.  Not specified.  If so, scope images are needed to make any useful recommendations.
Yes, the ringing is on Vge. I did attach scope shots, but I guess since they were not included in the post itself they were hard to see. Here they are again, the first with normal operation (signal generator) and the second with freewheeling:


Offline davekni

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Re: CM400 Induction Heater
« Reply #23 on: May 04, 2024, 08:56:27 PM »
Quote
Yes, the ringing is on Vge. I did attach scope shots, but I guess since they were not included in the post itself they were hard to see. Here they are again, the first with normal operation (signal generator) and the second with freewheeling:
Now I see those plots in your previous post.  For some reason only the top of your three images showed up the first time I read your earlier post.
Looks like ringing of UD+ output coupling capacitors with GDT parallel inductance.  Presuming UD+ output looks like that of UD2.7, there is a coupling capacitor paralleled by another capacitor with resistor in series.  Adjusting R/C values to be critically damped with your GDT inductance will make ringing die down faster.  Larger capacitors will reduce ring amplitude.
However, as you said, ring is small enough as is.  No fixing is necessary.
David Knierim

Offline Anders Mikkelsen

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Re: CM400 Induction Heater
« Reply #24 on: May 06, 2024, 04:20:37 PM »
Happy that you made nice use of the cap already.

For the heater, you definitely want the current sensing for overcurrent protection on the primary side of the coupling transformer. The capacitor will take minutes to overheat, while the IGBTs can fail in tens of microseconds if the current exceeds a safe value. The way you have it now, the magnetizing current, and its potential resonance with the coupling caps, draws current that is completely unmonitored. Current monitoring for the sake of control can still be kept on the secondary side, but keep in mind that the expected high currents in normal use will require a very substantial current sense transformer. If you have two 1:32 transformers, the current in the secondary of the first transformer will be over 30 A at the full 1 kA tank current. This is usually not a problem in DRSSTCs where the RMS current is in the 100 A ballpark, but in induction heaters when you have steady-state high current it can be problematic.

It also makes sense to measure Vce of the IGBTs in operation, to rule out overvoltage as a failure cause. The last problematic thing I can think of is potentially cross-conduction, and the resulting high current spikes and L*di/dt Vce overshoot, since the IGBTs take significantly longer to turn off than they take to turn on. Make sure you have sufficient dead-time to account for this. Does the controller implement dead-time, or is this only ensured by turn-on gate resistance vs turn-off gate resistance? The latter case is not ideal, as you would have to really slow down the turn-off to mitigate cross-conduction.

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Re: CM400 Induction Heater
« Reply #24 on: May 06, 2024, 04:20:37 PM »

 


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